Design evaluation of the fractured main landing gear of a BAE Jetstream SX-SKY aircraft

被引:0
|
作者
Chondrou, I. T. [1 ,2 ]
Mavrantonakis, G. [3 ]
Tsagarakis, N. [3 ]
Vergis, E. [3 ]
Pangalos, D. [3 ]
Chondros, T. G. [1 ]
机构
[1] Univ Patras, Dept Mech Engn & Aeronaut, Patras, Greece
[2] Emirates Grp, Dubai, U Arab Emirates
[3] Sky Express, SA Tech Dept, Iraklion, Greece
关键词
Fatigue; Design; Analytic methods; Fracture damage; Main landing gear mechanism; Safety implications;
D O I
暂无
中图分类号
T [工业技术];
学科分类号
08 ;
摘要
Purpose - The purpose of this paper is to study the main landing gear (MLG) mechanism configuration. Design/methodology/approach - Mechanism kinematics and dynamics, stress analysis and sizing of the MLG structural members, and fatigue issues related with the mechanism operation. Spreadsheet solutions were incorporated to this survey to analyze the most conceivable loading situations, and important factors of the mechanism design for an initial evaluation of safety implications. Findings - MlG design approach along with conservative fatigue design factors lies in the area of accepted limits in commercial aircraft industry. Research limitations/implications - MLG loading associated with landing as well as those associated with ground maneuvers (steering, braking and taxiing) contribute significantly to fatigue damage, along with the stresses induced by manufacturing processes and assembly. The application of FEA methods for the design of the landing gear does not always guarantee a successful approach to the problem solution, if precise analytical solutions are not available in advance. Practical implications - From the investigation of this incident of fractured struts of the MLG it is confirmed that the reduction in Pintle Housing diameter on the upper part has contributed to the avoidance of damaging the fuel tank above the MLG that would lead to a catastrophic event. On the other hand, the airframe of the SKY-Jet was proved efficient for a belly landing with minor damages to the passengers and heavier damages for the aircraft. Social implications - On-line vibration monitoring sensors hooked up to the landing gear strut and Pintle House would greatly enhance safety, without relying in optical surveys in hard to access and inspect areas of the landing gears mechanisms housings. Originality/value - Analytic methods were adopted and spreadsheet solutions were developed for the MLG main loading situations, along with design issues concerning mechanism kinematics and dynamics, stress analysis and sizing of the MLG structural members, as well as fatigue issues related with the mechanism operation. Spreadsheet solutions were incorporated to this survey to analyze the most conceivable loading situations, and important factors of the mechanism design for an initial evaluation of safety implications.
引用
收藏
页码:468 / 492
页数:25
相关论文
共 50 条
  • [31] Design and static analysis of landing gear shock absorber of commercial aircraft
    Sonowal, Plabita
    Pandey, K. M.
    Sharma, K. K.
    MATERIALS TODAY-PROCEEDINGS, 2021, 45 : 6712 - 6717
  • [32] Numerical continuation analysis of a three-dimensional aircraft main landing gear mechanism
    J. A. C. Knowles
    B. Krauskopf
    M. Lowenberg
    Nonlinear Dynamics, 2013, 71 : 331 - 352
  • [33] Effect of the impact load on the main welding outer cylinder of large aircraft landing gear
    Wang, H.F.
    Song, W.W.
    Wang, J.L.
    Zuo, D.W.
    Duan, X.L.
    Key Engineering Materials, 2013, 567 : 169 - 173
  • [34] Design optimization of aircraft landing gear assembly under dynamic loading
    Wong, J.
    Ryan, L.
    Kim, I. Y.
    STRUCTURAL AND MULTIDISCIPLINARY OPTIMIZATION, 2018, 57 (03) : 1357 - 1375
  • [35] Selection Methodology of Composite Material for Retractable Main Landing Gear Strut of a Lightweight Aircraft
    Ahmad, Muhammad Ayaz
    Rafiq, Hamza
    Shah, Syed Irtiza Ali
    Khan, Sabih Ahmad
    Rizvi, Syed Tauqeer ul Islam
    Shams, Taimur Ali
    APPLIED SCIENCES-BASEL, 2022, 12 (11):
  • [36] Simulations and Experiments of Hot Forging Design and Evaluation of the Aircraft Landing Gear Barrel Al Alloy Structure
    Prabhu, T. Ram
    JOURNAL OF MATERIALS ENGINEERING AND PERFORMANCE, 2016, 25 (04) : 1257 - 1268
  • [37] Simulations and Experiments of Hot Forging Design and Evaluation of the Aircraft Landing Gear Barrel Al Alloy Structure
    T. Ram Prabhu
    Journal of Materials Engineering and Performance, 2016, 25 : 1257 - 1268
  • [38] A Novel Framework for Qualification of a Composite-Based Main Landing Gear Strut of a Lightweight Aircraft
    Ahmad, Muhammad Ayaz
    Ali Shah, Syed Irtiza
    Khan, Sabih Ahmad
    Khan, Haris Ali
    Shams, Taimur Ali
    POLYMERS, 2023, 15 (06)
  • [39] Study of the Effect of Joint Gap on Malfunction of Aircraft Main Landing Gear through Sensitivity Analysis
    Cho, Sungjoon
    Kwon, Hyeok-jun
    Lee, Dooyoul
    Cho, Hwanjeong
    TRANSACTIONS OF THE KOREAN SOCIETY OF MECHANICAL ENGINEERS A, 2020, 44 (10) : 689 - 698
  • [40] New Material Development for Aircraft Landing Gears through Sumitomo's Landing Gear Design Experiences
    Takahashi, Norio
    Sato, Toyohiro
    Nakatsuka, Shinichi
    Iwai, Shoji
    PROCEEDINGS OF 2010 ASIA-PACIFIC INTERNATIONAL SYMPOSIUM ON AEROSPACE TECHNOLOGY, VOL 1 AND 2, 2010, : 954 - +