Process intensification in ternary distillation via comparative grassroots and retrofit designs: A case study of distilling an industrial multicomponent C6 alkane mixture in caprolactam processing

被引:7
作者
Cui, Chengtian [1 ]
Zhang, Xiaodong [2 ,3 ]
Lyu, Hao [2 ,3 ]
Wang, Shaojing [2 ,3 ]
Sun, Jinsheng [2 ,3 ]
Qu, Yaping [4 ,5 ]
Wu, Wangcheng [4 ,5 ]
Bo, Cuimei [6 ]
Wong, David Shan-Hill [7 ]
Zhang, Quanling [1 ]
机构
[1] Nanjing Tech Univ, Inst Intelligent Mfg, Nanjing 211816, Peoples R China
[2] Tianjin Univ, Joint Res Ctr Distillat Technol, Tianjin 300072, Peoples R China
[3] Tianjin Univ, Fujian Eversun Technol Co Ltd, Sch Chem Engn & Technol, Tianjin 300072, Peoples R China
[4] Tianjin Univ, Joint Res Ctr Distillat Technol, Shimenao Ind Pk, Xiuyu 351100, Putian, Peoples R China
[5] Fujian Eversun Technol Co Ltd, Shimenao Ind Pk, Xiuyu 351100, Putian, Peoples R China
[6] Nanjing Tech Univ, Coll Elect Engn & Control Sci, Nanjing 211816, Peoples R China
[7] Natl Tsing Hua Univ, Dept Chem Engn, Hsinchu 30013, Taiwan
基金
中国国家自然科学基金;
关键词
Multicomponent distillation; Process intensification; Grassroots design; Thermodynamic efficiency; Composition profile; Retrofit; WALL; CONFIGURATIONS; OPTIMIZATION; COLUMNS;
D O I
10.1016/j.cep.2021.108423
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
A systematic process intensification method via comparative grassroots and retrofit designs for distillation is proposed. Restricting to the ternary system, a case study of multicomponent C6 alkane separation in caprolactam processing is considered. The existing benchmark flowsheet of direct sequence (DS) features high economic cost but low thermodynamic efficiency. Through the investigation of the composition profile, two middle component remixing peaks and a large feed mismatch are diagnosed as the reasons of inefficiency. To achieve process intensification, potential candidates like side stream column (SSC) and dividing wall column (DWC) are enumerated and evaluated in the grassroots design step. Although DWC performs the best in thermodynamic efficiency, SSC is more preferred for retrofit as its structure is simple but has similar performance. To maximally reuse the existing equipment, two retrofit proposals of either indirect sequence (IS) or SSC are provided based on the grassroots design results. Among them, retrofitted SSC is recommended for long expected lifespan situation, while IS is more suitable for a short one. It is recommended that the proposed process intensification procedure can be extended to other similar processes or systems with more components, through enumerating and comparing the several best but similar grassroots designs with benchmark process.
引用
收藏
页数:22
相关论文
共 54 条
[31]  
Luyben W.L., 2011, Principles and Case Studies of Simultaneous Design
[32]  
Luyben WL, 2013, DISTILLATION DESIGN AND CONTROL USING ASPEN(TM) SIMULATION, 2ND EDITION, P1, DOI 10.1002/9781118510193
[33]   Superstructure modeling and stochastic optimization of side-stream extractive distillation processes for the industrial separation of benzene/cyclohexane/cyclohexene [J].
Lyu, Hao ;
Li, Shihan ;
Cui, Chengtian ;
Yu, Xingong ;
Sun, Jinsheng .
SEPARATION AND PURIFICATION TECHNOLOGY, 2021, 257
[34]  
Ng KM., 2017, PRODUCT PROCESS DESI, V4th ed.
[35]   Retrofit of distillation columns in biodiesel production plants [J].
Nguyen, Nghi ;
Demirel, Yasar .
ENERGY, 2010, 35 (04) :1625-1632
[36]   Intensified Distillation-Based Separation Processes: Recent Developments and Perspectives [J].
Nguyen Van Duc Long ;
Le Quang Minh ;
Ahmad, Faizan ;
Luis, Patricia ;
Lee, Moonyong .
CHEMICAL ENGINEERING & TECHNOLOGY, 2016, 39 (12) :2183-2195
[37]   Optimal retrofit of a side stream column to a dividing wall column for energy efficiency maximization [J].
Nguyen Van Duc Long ;
Lee, Moonyong .
CHEMICAL ENGINEERING RESEARCH & DESIGN, 2013, 91 (12) :2291-2298
[38]  
PETLYUK FB, 1965, INT CHEM ENG, V5, P555
[39]  
Rangaiah G.P., 2016, Chemical process retrofitting and revamping: techniques and applications
[40]  
Rangaiah GP, 2010, STOCHASTIC GLOBAL OP