Performance Enhancement of a Low Speed Axial Compressor Utilizing Simultaneous Tip Injection and Casing Treatment of Groove Type

被引:3
作者
Taghavi-Zenouz, Reza [1 ]
Behbahani, Mohammad Hosein Ababaf [1 ]
机构
[1] Iran Univ Sci & Technol, Sch Mech Engn, Tehran 1684613114, Iran
关键词
Axial compressor; Stall inception; Tip injection; Casing treatment; Stall margin; LEAKAGE FLOW; ROTOR;
D O I
10.5139/IJASS.2017.18.1.91
中图分类号
V [航空、航天];
学科分类号
08 ; 0825 ;
摘要
Performance of a low speed axial compressor is enhanced through a proper configuration of blade row tip injection and casing treatment of groove type. Air injectors were mounted evenly spaced upstream of the blade row within the casing groove and were all aligned parallel to the compressor axis. The groove, which covers all the blade tip chord length, extends all-round the casing circumference. Method of investigation is based on solution of the unsteady form of the Navier-Stokes equations utilizing k-omega SST turbulence model. Extensive parametric studies have been carried out to explore effects of injectors' flow momentums and yaw angles on compressor performance, while being run at different throttle valve setting. Emphasis has been focused on situations near to stall condition. Unsteady numerical analyses for untreated casing and no-injection case for near stall condition provided to discover two well-known criteria for spike stall inception, i.e., blade leading edge spillage and trailing edge back-flow. Final results showed that with only 6 injectors mounted axially in the casing groove and at yaw angle of 15 degrees opposite the direction of the blade row rotation, with a total mass flow rate of only 0.5% of the compressor main flow, surprisingly, the stall margin improves by 15.5%.
引用
收藏
页码:91 / 98
页数:8
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