Impact of Chemical Cleaning on Furnace Exit Gas Temperature of Power Plant:Case Study Steam Power Plant Unit 1

被引:0
|
作者
Silalahi, Netha A. M. [1 ]
Widanarko, Baskoro [2 ]
Jaganathan, Saravana Kumar [3 ]
机构
[1] Indonesia Power Co Ltd, Power Generat Engn, Jakarta, Indonesia
[2] Indonesia Power Co Ltd, Maintenance Serv Unit, Jakarta, Indonesia
[3] Univ Hull, Fac Engn, Kingston Upon Hull, N Humberside, England
关键词
chemical cleaning; superheater; furnace exit gas temperature;
D O I
10.1109/CPEEE51686.2021.9383340
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
Superheater as a part of thermal steam power plant could be damaged by deposit. If there is no significant degradation of material, in concern of reliability of power plant, the deposit could be removed by chemical cleaning. Alkali chemical cleaning is chosen since the material is sensitive to low pH and the chemical composition of deposit analysis. Process parameter is monitored continuously. After chemical treatment, there is even distribution of temperature on superheater tubes describes the better heat distribution at superheater tubes (Delta T = 10 - 25 degrees C) and also Furnace Exit Gas Temperature (Delta T = 50 degrees C) reduced significantly indicating the better heat transfer in boiler. Improvement of heat transfer of boiler as the result of proper chemical cleaning maybe beneficial in improving the boiler efficiency
引用
收藏
页码:182 / 188
页数:7
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