Impact of Chemical Cleaning on Furnace Exit Gas Temperature of Power Plant:Case Study Steam Power Plant Unit 1

被引:0
|
作者
Silalahi, Netha A. M. [1 ]
Widanarko, Baskoro [2 ]
Jaganathan, Saravana Kumar [3 ]
机构
[1] Indonesia Power Co Ltd, Power Generat Engn, Jakarta, Indonesia
[2] Indonesia Power Co Ltd, Maintenance Serv Unit, Jakarta, Indonesia
[3] Univ Hull, Fac Engn, Kingston Upon Hull, N Humberside, England
关键词
chemical cleaning; superheater; furnace exit gas temperature;
D O I
10.1109/CPEEE51686.2021.9383340
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
Superheater as a part of thermal steam power plant could be damaged by deposit. If there is no significant degradation of material, in concern of reliability of power plant, the deposit could be removed by chemical cleaning. Alkali chemical cleaning is chosen since the material is sensitive to low pH and the chemical composition of deposit analysis. Process parameter is monitored continuously. After chemical treatment, there is even distribution of temperature on superheater tubes describes the better heat distribution at superheater tubes (Delta T = 10 - 25 degrees C) and also Furnace Exit Gas Temperature (Delta T = 50 degrees C) reduced significantly indicating the better heat transfer in boiler. Improvement of heat transfer of boiler as the result of proper chemical cleaning maybe beneficial in improving the boiler efficiency
引用
收藏
页码:182 / 188
页数:7
相关论文
共 50 条
  • [1] Chemical steam generator cleaning at Unterweser Nuclear Power Plant
    Kostroun, F.
    Kuhnke, K.
    Hollwedel, Ursula
    VGB Kraftwerkstechnik, 1995, 75 (09):
  • [2] Conversion of steam power plant into cogeneration unit-Case study
    Panowski, Marcin
    Zarzycki, Robert
    Kobylecki, Rafal
    ENERGY, 2021, 231
  • [3] STEAM POWER UNIT WITH A PEAK LOAD GAS-TURBINE PLANT
    KIRILLOV, II
    POLISHCHUK, VL
    ARSENEV, LV
    THERMAL ENGINEERING, 1974, 21 (03) : 15 - 18
  • [4] Energy and exergy analysis of dry-steam geothermal power plant: Case study in kamojang geothermal power plant unit 2
    Setyawan, Nova Dany
    Pambudi, Nugroho Agung
    Utomo, Frandhoni
    Saputro, Herman
    Adiprana, Reza
    Saw, Lip Huat
    Gurturk, Mert
    Rudiyanto, Bayu
    3RD ANNUAL APPLIED SCIENCE AND ENGINEERING CONFERENCE (AASEC 2018), 2018, 197
  • [5] High-Temperature Combined Gas and Steam Power Plant.
    Kirillov, I.I.
    1978, (04): : 5 - 6
  • [6] Chemical Cleaning of Steam Power Boilers: Operational Need for Normal Plant Operation.
    Rossi, Bruno
    Termotecnica Milano, 1987, 41 (04): : 47 - 52
  • [7] Analysis Heat Exchanger Network Steam Power Plant in Using Pinch (Case Study in PT POMI Unit 3 Power Plant Paiton)
    Rudiyanto, Bayu
    Raga, Titah
    Prasetyo, Totok
    Rahmanto, Dedi
    Nuruddin, Mochammad
    Pambudi, Nugroho
    Wibowo, Kukuh
    INTERNATIONAL JOURNAL OF HEAT AND TECHNOLOGY, 2020, 38 (02) : 439 - 446
  • [8] Online monitoring of furnace exit gas temperature in power plants
    Zhang, Shiping
    Shen, Guoqing
    An, Liansuo
    APPLIED THERMAL ENGINEERING, 2019, 147 : 917 - 926
  • [9] Comparative thermodynamic and economic analysis of a conventional gas-steam power plant with a modified gas-steam power plant
    Bartnik, Ryszard
    Buryn, Zbigniew
    Hnydiuk-Stefan, Anna
    ENERGY CONVERSION AND MANAGEMENT, 2023, 293
  • [10] Exergy analysis of a gas turbine cycle power plant: a case study of power plant in Egypt
    Elwardany, Mohamed
    Nassib, A. M.
    Mohamed, Hany A.
    JOURNAL OF THERMAL ANALYSIS AND CALORIMETRY, 2024, 149 (14) : 7433 - 7447