EVOLUTION OF GAS TURBINE INTAKE AIR FILTRATION IN A 420 MW COGENERATION PLANT

被引:0
|
作者
Ingistov, Steve [1 ]
Milos, Michael [1 ]
Bhargava, Rakesh K. [2 ]
机构
[1] Tesoro WCC, Carson, CA 90745 USA
[2] Innovat Turbomachinery Technol Corp, Katy, TX USA
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暂无
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
A suitable inlet air filter system is required for a gas turbine, depending on installation site and its environmental conditions, to minimize contaminants entering the compressor section in order to maintain gas turbine performance. This paper describes evolution of inlet air filter systems utilized at the 420 MW Watson Cogeneration Plant consisting of four GE 7EA gas turbines since commissioning of the plant in November 1987. Changes to the inlet air filtration system became necessary due to system limitations, a desire to reduce operational and maintenance costs, and enhance overall plant performance. Based on approximately 2 years of operational data with the latest filtration system combined with other operational experiences of more than 25 years, it is shown that implementation of the high efficiency particulate air filter system provides reduced number of crank washes, gas turbine performance improvement and significant economic benefits compared to the traditional synthetic media type filters. Reasons for improved gas turbine performance and associated economic benefits, observed via actual operational data, with use of the latest filter system are discussed in this paper.
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页数:8
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