Modeling of Steam Turbine's Governing System during Main Steam Valve Activity Test and its Application

被引:0
作者
Sheng Kai [1 ]
Zheng Zhong [2 ]
Zhou Nianguang [3 ]
Xun Xin [1 ]
机构
[1] State Grid Hunan Elect Power Cor, Res Inst, Changsha 410007, Hunan, Peoples R China
[2] Hunan Xiangdian Test & Res Inst Co Ltd, Changsha 410007, Hunan, Peoples R China
[3] State Grid Hunan Elect Power Corp, Changsha 410007, Hunan, Peoples R China
来源
PROCEEDINGS OF THE 36TH CHINESE CONTROL CONFERENCE (CCC 2017) | 2017年
关键词
main steam valve activity test; load fluctuation; steam turbine; governing system; optimization;
D O I
暂无
中图分类号
TP [自动化技术、计算机技术];
学科分类号
0812 ;
摘要
Model of a 300MW thermal power unit's governing system of steam turbine was established to analyze its load fluctuation during main steam valve activity test. The model contains three sub-models. They are model of turbine's governor during main steam valve activity test, model of governing valve, model of steam turbine considering governing valve's discharge characteristic. Based on the established model, the cause of load fluctuation and optimization method were determined. Then the optimization method was applied to actual main steam valve activity test. The test result indicated that load fluctuation was obviously suppressed after optimization.
引用
收藏
页码:2166 / 2171
页数:6
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