Wake generator control of inlet flow to cancel flow distortion noise

被引:9
|
作者
Kota, V. [1 ]
Wright, M. C. M. [1 ]
机构
[1] Univ Southampton, Inst Sound & Vibrat Res, Southampton SO17 1BJ, Hants, England
基金
英国工程与自然科学研究理事会;
关键词
D O I
10.1016/j.jsv.2005.12.050
中图分类号
O42 [声学];
学科分类号
070206 ; 082403 ;
摘要
If the inlet flow to a fan is non-uniform, as is often the case for aircraft engines, then undesirable tonal noise can be generated. A number of authors have suggested using active cancellation to reduce the noise. The secondary field can either be generated by loudspeakers or by the fan itself if secondary non-uniformities are deliberately introduced into the flow. In the research reported here rods inserted radially into the duct were used to generate the secondary field. The distance by which each rod protrudes into the duct was adaptively adjusted in response to an array of in-duct microphones so as to minimise the radiated sound power, whereas previously only fixed rods have been considered. The ability of the steepest-descent algorithm to minimise in-duct sound power under suitable conditions, and hence reduce radiated sound power is demonstrated in both simulations and low Mach number experiments. It is shown how the ability of such a system to control noise depends on the number and position of the controller rods, and the number of acoustic duct modes to be controlled. Thus at low fan speed, when only one mode was present just two controllers achieved an in-duct noise reduction of 25 dB at the blade passing frequency, whereas at a higher fan speed with three modes present six controllers only achieved 2 dB. To implement such a scheme in practice, where large numbers of modes are typically present, it would be necessary to develop controller arrays with many actuators, but with low aerodynamic penalty. Such a system might also be useful in HVAC applications, or in wind-tunnel testing. (c) 2006 Elsevier Ltd. All rights reserved.
引用
收藏
页码:94 / 113
页数:20
相关论文
共 50 条
  • [1] STUDY ON VORTEX GENERATOR FLOW-CONTROL FOR THE MANAGEMENT OF INLET DISTORTION
    ANDERSON, BH
    GIBB, J
    JOURNAL OF PROPULSION AND POWER, 1993, 9 (03) : 422 - 430
  • [2] AXIAL-FLOW FAN NOISE CAUSED BY INLET FLOW DISTORTION
    MUGRIDGE, BD
    JOURNAL OF SOUND AND VIBRATION, 1975, 40 (04) : 497 - 512
  • [3] Investigation on flow distortion control of a subsonic inlet
    Wang, Jian
    Li, Ying-Hong
    Zhang, Bai-Ling
    Tuijin Jishu/Journal of Propulsion Technology, 2010, 31 (02): : 143 - 146
  • [4] STUDY ON VORTEX FLOW-CONTROL OF INLET DISTORTION
    ANDERSON, BH
    HUANG, PS
    PASCHAL, WA
    CAVATORTA, E
    JOURNAL OF PROPULSION AND POWER, 1992, 8 (06) : 1266 - 1272
  • [5] INLET FLOW DISTORTION IN TURBOMACHINERY
    SEIDEL, BS
    MATWEY, MD
    ADAMCZYK, JJ
    JOURNAL OF ENGINEERING FOR POWER-TRANSACTIONS OF THE ASME, 1980, 102 (04): : 924 - 929
  • [6] StreamVane Turbofan Inlet Swirl Distortion Generator: Mean Flow and Turbulence Structure
    Guimaraes, Tamara
    Lowe, K. Todd
    O'Brien, Walter F.
    JOURNAL OF PROPULSION AND POWER, 2018, 34 (02) : 340 - 353
  • [7] Strip distortion generator for simulating inlet flow distortion in gas turbine engine ground test facilities
    Yusoof, M. Saleem
    Sivapragasam, M.
    Deshpande, M. D.
    PROPULSION AND POWER RESEARCH, 2016, 5 (04) : 287 - 301
  • [8] FLOW CONTROL IN SERPENTINE INLET DUCT USING VORTEX GENERATOR JETS
    Sullerey, R. K.
    Chandra, S.
    PROCEEDINGS OF THE ASME FLUIDS ENGINEERING DIVISION SUMMER CONFERENCE -2008, VOL 1, PT A AND B, 2009, : 493 - 497
  • [9] INLET AIR-FLOW DISTORTION IN TURBOMACHINERY
    TANIDA, Y
    ZEITSCHRIFT FUR ANGEWANDTE MATHEMATIK UND PHYSIK, 1972, 23 (04): : 645 - 654
  • [10] Investigation of distortion simulator for inlet flow field
    Yu, A.Y.
    Wang, Q.F.
    Hangkong Dongli Xuebao/Journal of Aerospace Power, 2001, 16 (02):