Effect of Bed Pressure Drop on Performance of a CFB Boiler

被引:41
作者
Yang, Hairui [1 ]
Zhang, Hai [1 ]
Yang, Shi [1 ]
Yue, Guangxi [1 ]
Su, Jun [2 ]
Fu, Zhiping [3 ]
机构
[1] Tsinghua Univ, Dept Thermal Engn, Key Lab Thermal Sci & Power Engn, Minist Educ, Beijing 100084, Peoples R China
[2] Taiyuan Boiler Grp Co Ltd, Taiyuan 030021, Peoples R China
[3] Shanxi Lishi Datuhe Heat & Power Cogenerat, Lishi 033000, Peoples R China
关键词
CIRCULATING FLUIDIZED-BED; FLOW REGIMES; BALANCE; LOOP; ASH;
D O I
10.1021/ef900025h
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
The effect of bed pressure drop and bed inventory on the performances of a circulating fluidized bed (CFB) boiler was studied. By using the state specification design theory, the fluidization state of the gas-solids flow in the furnace of conventional CFB boilers was reconstructed to operate at a much lower bed pressure drop by reducing bed inventory and control bed quality. Through theoretical analysis, it was suggested that there would exist a theoretical optimal value of bed pressure drop, around which the boiler operation can achieve the maximal combustion efficiency and with significant reduction of the wear of the heating surface and fan energy consumption. The analysis was validated by field tests carried out in a 75 t/h CFB boiler. At full boiler load, when bed pressure drop was reduced from 7.3 to 3.2 kPa, the height of the dense zone in the lower furnace decreased, but the solid suspension density profile in the upper furnace and solid flow rate were barely influenced. Consequently, the average heat transfer coefficient in the furnace was kept nearly the same and the furnace temperature increment was less than 17 degrees C. It was also found that the carbon content in the fly ash decreased first with decreasing bed pressure drop and then increased with further increasing bed pressure drop. The turning point with minimal carbon content was referred to as the point with optimal bed pressure drop. For this boiler, at the optimum point the bed pressure was around 5.7 kPa with the overall excess air ratio of 1.06. When the boiler was operated around this optimal point, not only the combustion efficiency was improved, but also fan energy consumption and wear of heating surface were reduced.
引用
收藏
页码:2886 / 2890
页数:5
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