Experimental investigation on the combustion behaviour of pre-dried Greek lignite

被引:40
作者
Agraniotis, Michalis [1 ]
Grammelis, Panagiotis [1 ,2 ]
Papapavlou, Charalambos [3 ]
Kakaras, Emmanuel [1 ,2 ]
机构
[1] Natl Tech Univ Athens, Sch Mech Engn, Lab Steam Boilers & Thermal Plants, Zografos 15780, Greece
[2] Ctr Res & Technol Hellas, Inst Solid Fuels Technol & Applicat, Ptolemais, Greece
[3] Publ Power Corp SA, Athens, Greece
关键词
Dry lignite; Temperature profiles; Emissions; Deposition; ASH;
D O I
10.1016/j.fuproc.2009.04.015
中图分类号
O69 [应用化学];
学科分类号
081704 ;
摘要
The present paper includes the results of the combustion tests with Greek dried lignite performed at a 1 MWth semi industrial scale pulverized coal combustion facility. Scope of the campaign is the investigation of the combustion behaviour of Greek lignite, i.e. temperature fields, ignition, burnout, emissions, as well as slagging and fouling tendency, while firing with varying levels of recirculated flue gas. Dry coal co-firing conditions in a large scale boiler are simulated by adjusting the volume flow of recirculated flue gas. Two test series representing different boiler operation modes are performed. During the first series the maximum flue gas temperature increase, when co-firing dry coal, is determined, while in the second test series the needed load decrease. in order to keep constant furnace outlet temperature in dry coal co-firing conditions is recorded. A detailed measurement set is carried out including temperature profiles, emissions, fuel, fly ash sampling and slagging and fouling investigations through the installation of dedicated deposition probes. The anticipated increase of the furnace temperature profiles by decreasing the inserted recirculated flue gas is confirmed by the experimental results. No clear trend of dry coal co-combustion on the emissions' behaviour is noticed, while dry coal firing appears to have a moderate effect on the deposition behaviour of Greek lignite. These preliminary investigations indicate that no significant operational problems are expected during a potential future demonstration of dry lignite co-firing in a Greek large scale boiler. (C) 2009 Elsevier B.V. All rights reserved.
引用
收藏
页码:1071 / 1079
页数:9
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