Field Measurements on the Emission and Removal of PM2.5 from Coal-Fired Power Stations: 1. Case Study for a 1000 MW Ultrasupercritical Utility Boiler

被引:51
|
作者
Liu, Xiaowei [1 ]
Xu, Yishu [1 ]
Zeng, Xianpeng [1 ]
Zhang, Yu [1 ]
Xu, Minghou [1 ]
Pan, Siwei [2 ]
Zhang, Kai [2 ]
Li, Li [2 ]
Gao, Xiangpeng [3 ]
机构
[1] Huazhong Univ Sci & Technol, State Key Lab Coal Combust, Luoyu Rd 1037, Wuhan 430074, Peoples R China
[2] Guangdong Power Grid Corp, Elect Power Res Inst, Guangzhou 510080, Guangdong, Peoples R China
[3] Murdoch Univ, Sch Engn & Informat Technol, Discipline Elect Engn Energy & Phys, 90 South St, Murdoch, WA 6150, Australia
基金
中国国家自然科学基金;
关键词
FLUE-GAS DESULFURIZATION; PARTICULATE MATTER; ELECTROSTATIC PRECIPITATORS; SIZE DISTRIBUTION; FLY-ASH; CHEMICAL-COMPOSITION; FINE PARTICLES; TRACE-ELEMENTS; SO2; OXIDATION; COMBUSTION;
D O I
10.1021/acs.energyfuels.6b00423
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
Enlarging the capacity of Utility boiler is recognized. as 4 good way to improve the electricity generating efficiency. An increasing number of 1000 MW ultrasupercritical (USC) utility boilers are installed in China. This contribution reports the results of systematic field measurements on PM2.5 [particulate matter (PM) with aerodynamic diameters < 2.5 mu m] emitted from a 1000 MW USC utility boiler equipped with a selective catalytic reduction (SCR) denitrification (DeNO(x)) unit, two electrostatic precipitators (ESPs), and a limestone-gypsum wet flue gas desulfurization (WFGD) system. The PM samples were collected using a Dekati low pressure impactor (DLPI) and/or a Dekati gravimetric impactor (DGI) at multiple sampling sites. The results demonstrate that the particle size distributions (PSDs) of the PM at both inlet and outlet of the SCR unit exhibit a bimodal distribution, with,a fine mode at < 0.3 mu m and a coarse mode at > 0.3 mu m. Passing the PM-containing flue gas through the SCR leads to the PSDs of the fine mode particles being shifted to larger size, possibly due to the formation of ammonium sulfate and/or ammonium bisulfate as well as the reduction of flue gas temperature. The removal efficiencies of the SCR for PM1 and PM2.5 are 14.3-33.6% and 13.3-30.5%, respectively, depending on the boiler load. The ESPs substantially reduce the mass concentrations of PM1 and PK2.5 from 84.6-107 mg/Nm(3) and 417-440 mg/Nm(3) to 0.298-1.22 mg/Nm(3) and 0.812-4.41 mg/Nm(3), respectively, with overall removal efficiencies of 98.7-99.7% for PM1 and 99.0-99.8%, for PM2.5. The WFGD process leads to the disappearance of the fine mode PM and an overall removal efficiencies of up to 28.7% for PM1 and 39.6% for PM2.5. Moreover, promoting the installation of 1000 MW USC utility boilers is likely to simultaneously achieve the reduction in the PM2.5 emission besides the improvement of electricity generation efficiency, particularly when advanced dust removal devices are employed.
引用
收藏
页码:6547 / 6554
页数:8
相关论文
共 50 条
  • [21] Cardiovascular impact of PM2.5 from the emissions of coal-fired power plants in Spain during 2014
    Ruiz Bautista, Lorena
    MEDICINA CLINICA, 2019, 153 (03): : 100 - 105
  • [22] Assessment and offset of the adverse effects induced by PM2.5 from coal-fired power plants in China
    He, Chengyu
    Huang, Guohe
    Liu, Lirong
    Li, Yongping
    Zhai, Mengyu
    Cao, Rong
    JOURNAL OF CLEANER PRODUCTION, 2021, 286
  • [23] Effects of APCDs on PM emission: A case study of a 660 MW coal-fired unit with ultralow pollutants emission
    Ruan, Renhui
    Liu, Hexin
    Tan, Houzhang
    Yang, Fuxin
    Li, Yan
    Duan, Yufeng
    Zhang, Sicong
    Lu, Xuchao
    APPLIED THERMAL ENGINEERING, 2019, 155 : 418 - 427
  • [24] Experimental study on emission characteristics and formation mechanisms of PM10from a coal-fired boiler
    State Key Laboratory of Coal Combustion, Huazhong University of Sci. and Tech., Wuhan 430074, China
    不详
    Zhongguo Dianji Gongcheng Xuebao, 2007, 17 (11-17):
  • [25] Simulating changes in source profiles from coal-fired power stations:: Use in chemical mass balance of PM2.5 in the Mount Zirkel Wilderness
    Watson, JG
    Chow, JC
    Lowenthal, DH
    Robinson, NF
    Cahill, CF
    Blumenthal, DL
    ENERGY & FUELS, 2002, 16 (02) : 311 - 324
  • [26] Experimental study on emission characteristics and elemental composition of PM10 from a coal-fired boiler
    Sui, Jian-Cai
    Xu, Ming-Hou
    Qiu, Ji-Hua
    Guo, Xin
    Gao, Xiang-Peng
    Wang, Quan-Bin
    Cao, Qian
    Ranshao Kexue Yu Jishu/Journal of Combustion Science and Technology, 2006, 12 (05): : 432 - 437
  • [27] Source profile and health risk assessment of PM2.5 from coal-fired power plants in Fuxin, China
    Xiaoliang Zhao
    Yunbin Liu
    Fangwei Han
    Bilal Touseef
    Yangxia Yue
    Jing Guo
    Environmental Science and Pollution Research, 2021, 28 : 40151 - 40159
  • [28] Source profile and health risk assessment of PM2.5 from coal-fired power plants in Fuxin, China
    Zhao, Xiaoliang
    Liu, Yunbin
    Han, Fangwei
    Touseef, Bilal
    Yue, Yangxia
    Guo, Jing
    ENVIRONMENTAL SCIENCE AND POLLUTION RESEARCH, 2021, 28 (30) : 40151 - 40159
  • [29] Development of advanced electrostatic precipitation technologies for reducing PM2.5 emissions from coal-fired power plants
    Xiong, Guilong
    Li, Shuiqing
    Chen, Sheng
    Zhang, Xuhui
    Yao, Qiang
    Zhongguo Dianji Gongcheng Xuebao/Proceedings of the Chinese Society of Electrical Engineering, 2015, 35 (09): : 2217 - 2223
  • [30] Impact of “ultra low emission” technology of coal-fired power on PM2.5 pollution in the Jing-Jin-Ji Region
    Xiao Liu
    Zhilin Liu
    Weidong Jiao
    Xuan Li
    Jintai Lin
    Anthony Ku
    Frontiers in Energy, 2021, 15 : 235 - 239