Generator step-up transformer post mortem assessment

被引:13
|
作者
Susa, D. [1 ]
Liland, K. B. [1 ]
Lundgaard, L. [1 ]
Vardal, G. [2 ]
机构
[1] SINTEF Energy Res, Elect Power Technol, NO-7465 Trondheim, Norway
[2] Sira Kvina Kraftselskaf, N-4441 Tonstad, Norway
来源
关键词
DP; hot-spot temperature; relative aging rate; step-up generator transformer; top-oil temperature; POWER TRANSFORMERS; PAPER INSULATION;
D O I
10.1002/etep.544
中图分类号
TM [电工技术]; TN [电子技术、通信技术];
学科分类号
0808 ; 0809 ;
摘要
The condition assessment of the 190 MVA, OFWF, step-up generator transformer was performed by the mapping of degree of polymerization (DP). The transformer was taken out of service after 36 years and the active part, (transformer core and windings), was removed from the tank for close examination due to the major thermal fault at the transformer core. The transformer insulation consisted of two different materials, i.e. winding insulation was the thermally upgraded paper and spacer-pressboard system was Kraft paper. The temperature mapping is also shown, where the temperature estimation is based on the paper aging kinetics, transformer loading and insulation operating history. New equation for the relative aging rate is given considering all insulation conditions providing possibility of counting transformer loss-of-life more accurately. Copyright (C) 2010 John Wiley & Sons, Ltd.
引用
收藏
页码:1802 / 1822
页数:21
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