Axial Impulse Generation of Lightcraft Engines with ∼ 1 μs Pulsed TEA CO2 Laser

被引:0
作者
Kenoyer, D. A. [1 ]
Salvador, I. I. [1 ]
Myrabo, L. N. [1 ]
机构
[1] Rensselaer Polytech Inst, Dept Mech Aeronaut & Nucl Engn, Troy, NY 12181 USA
来源
BEAMED ENERGY PROPULSION: SEVENTH INTERNATIONAL SYMPOSIUM | 2011年 / 1402卷
关键词
Lasers; Lightcraft; Laser propulsion;
D O I
10.1063/1.3657018
中图分类号
O59 [应用物理学];
学科分类号
摘要
A twin Lumonics K922M pulsed TEA CO2 laser system (similar to 50 ns FWHM spike, with selectable 1.5 or 2.5 mu s tail-depending upon laser gas mixture) was employed to experimentally measure the axial impulse behavior of a family of lightcraft engine geometries, using a lightweight ballistic pendulum. Axial impulse performance in both airbreathing and solid ablative rocket (SAR) modes was examined as a function of: a) laser pulse energy (similar to 12 to 40 Joules); b) pulse duration (similar to 50 ns spike with 1.5 or 2.5 mu s tail); and, c) engine geometry. The four engines under investigation were the Lightcraft Types #150, #200 and #250, and a 11 cm parabolic bell. Lightcraft #200 axial C-M performance reached 250 N/MW, which is sharply higher than the 120 N/MW previously reported for the engine using long pulse (e.g., 10-18 mu s) CO2 electric discharge lasers.
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页数:11
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