Optimization method for systematically improving non-contact R test accuracy

被引:6
作者
Jiang, Lei [1 ]
Peng, Bingkang [1 ]
Ding, Guofu [1 ]
Qin, Shengfeng [2 ]
Zhang, Jian [1 ]
Li, Yong [1 ]
机构
[1] Southwest Jiaotong Univ, Sch Mech Engn, Inst Adv Design & Mfg, Chengdu 610031, Sichuan, Peoples R China
[2] Northumbria Univ, Sch Design, Newcastle Upon Tyne NE1 8ST, Tyne & Wear, England
关键词
Optimization method; Non-contact R test; Structural parameter; On-machine calibration; Measurement accuracy; ROTARY AXES; CALIBRATION; ERRORS; MODEL;
D O I
10.1007/s00170-020-04999-3
中图分类号
TP [自动化技术、计算机技术];
学科分类号
0812 ;
摘要
Non-contact R test is an instrument to measure the synchronous errors of five-axis machine tools. However, there are still some deficiencies in its researches, such as the difficult and laborious calibrations. How to systematically improve the measurement accuracy with a good balance to minimum cost is a real problem in guiding practice. This paper proposes a new systematic optimization method to solve this problem based on a comprehensive understanding of the non-contact R test in terms of structure parameters and relations. Firstly, the algorithm for sphere center coordinates is established based on the self-adaptive differential evolution algorithm to obtain the definite computational accuracy and efficiency. Secondly, the parameters of the fixture structure are optimized to maximize the measurement stability, measuring space, and non-interference space. Thirdly, the on-machine calibration is performed to replace pre-calibration and re-calibration and to establish the positional relationships between sensors, the fixture, and the machine tool simultaneously. It can reduce the difficulties of manufacture, maintenance, and application. Fourthly, the measurement accuracy can be evaluated to determine whether the iterative optimization achieves the goal. The proposed method has been verified with case studies to support the setting-up of the optimized non-contact R test, leading to a cost-effective and accurate test on five-axis machine tools.
引用
收藏
页码:1697 / 1711
页数:15
相关论文
共 29 条
[11]   Dynamic R-test for rotary tables on 5-axes machine tools [J].
Florussen, G. H. J. ;
Spaan, H. A. M. .
FIFTH CIRP CONFERENCE ON HIGH PERFORMANCE CUTTING 2012, 2012, 1 :536-539
[12]  
Florussen GHJ, 2009, LAMD C 9
[13]   Non-contact R-test with laser displacement sensors for error calibration of five-axis machine tools [J].
Hong, Cefu ;
Ibaraki, Soichi .
PRECISION ENGINEERING-JOURNAL OF THE INTERNATIONAL SOCIETIES FOR PRECISION ENGINEERING AND NANOTECHNOLOGY, 2013, 37 (01) :159-171
[14]   Graphical presentation of error motions of rotary axes on a five-axis machine tool by static R-test with separating the influence of squareness errors of linear axes [J].
Hong, Cefu ;
Ibaraki, Soichi ;
Oyama, Chiaki .
INTERNATIONAL JOURNAL OF MACHINE TOOLS & MANUFACTURE, 2012, 59 :24-33
[15]   Influence of position-dependent geometric errors of rotary axes on a machining test of cone frustum by five-axis machine tools [J].
Hong, Cefu ;
Ibaraki, Soichi ;
Matsubara, Atsushi .
PRECISION ENGINEERING-JOURNAL OF THE INTERNATIONAL SOCIETIES FOR PRECISION ENGINEERING AND NANOTECHNOLOGY, 2011, 35 (01) :1-11
[16]   Construction of an error map of rotary axes on a five-axis machining center by static R-test [J].
Ibaraki, Soichi ;
Oyama, Chiaki ;
Otsubo, Hisashi .
INTERNATIONAL JOURNAL OF MACHINE TOOLS & MANUFACTURE, 2011, 51 (03) :190-200
[17]  
Ihara Y., 2011, INT J AUTO TECH-JPN, V5, P847, DOI [10.20965/ijat.2011.p0847, DOI 10.20965/IJAT.2011.P0847]
[18]  
JCGM ISO, 2012, ISO230-1
[19]   Posture adjustment of workpiece based on stepwise matching by self-adaptive differential evolution algorithm [J].
Jiang, Lei ;
Li, Yong ;
Zou, Yisheng ;
Tang, Kun ;
Fu, Yulong ;
Ma, Shuwen .
MECHANICAL SCIENCES, 2018, 9 (02) :267-276
[20]   Geometric error model and measuring method based on worktable for five-axis machine tools [J].
Jiang, Lei ;
Ding, Guofu ;
Li, Zhuang ;
Zhu, Shaowei ;
Qin, Shengfeng .
PROCEEDINGS OF THE INSTITUTION OF MECHANICAL ENGINEERS PART B-JOURNAL OF ENGINEERING MANUFACTURE, 2013, 227 (B1) :32-44