Performance evaluation and optimisation of post combustion CO2 capture processes for natural gas applications at pilot scale via a verified rate-based model

被引:20
作者
Rezazadeh, Fatemeh [1 ]
Gale, William F. [1 ]
Akram, Muhammad [2 ]
Hughes, Kevin J. [2 ]
Pourkashanian, Mohamed [2 ]
机构
[1] Univ Leeds, CIER, Sch Chem & Proc Engn, Leeds LS2 9JT, W Yorkshire, England
[2] Univ Sheffield, Dept Mech Engn, Sheffield S1 3JD, S Yorkshire, England
基金
英国工程与自然科学研究理事会;
关键词
Post-combustion CO2 capture; Energy consumption; Specific energy requirement; Total equivalent work; MEA; REACTIVE ABSORPTION; FLASH STRIPPER; SIMULATION; CONFIGURATIONS; SENSITIVITY;
D O I
10.1016/j.ijggc.2016.08.003
中图分类号
X [环境科学、安全科学];
学科分类号
08 ; 0830 ;
摘要
CO2 absorption based on chemical reactions is one of the most promising technologies for post combustion CO2 capture (PCC). There have been significant efforts to develop energy efficient and cost effective PCC processes. Given that PCC is still maturing as a technology, there will be a continuing need for pilot scale facilities to support process optimisation, especially in terms of energy efficiency. Pilot scale PCC facilities, which are usually orders of magnitude smaller than those that will be used in future in large scale fossil power plants, make it possible to study details of the PCC process at an affordable scale. However, it is essential that pilot scale studies provide credible data, if this is to be used with confidence to envisage the future large-scale use of the PCC process, especially in terms of energy consumption. The present work therefore establishes and experimentally verifies (using a representative pilot plant as a case study) procedures for analysing the energy performance of a pilot scale amine based CO2 capture plants, focusing on natural gas fired applications. The research critically assesses the pilot plant's current energy performance, and proposes new operating conditions and system modifications by which the pilot plant will operate more efficiently in terms of energy consumption. The methodology developed to assess and improve the energy performance of the PCC process is applicable, with appropriate inputs, to other plants of this type that employs aqueous 30 wt.% monoethanolamine (MEA) solution as the solvent. A rate based model of the post combustion CO2 capture process using an aqueous solution of 30 wt.% MEA as the solvent was developed in Aspen Plus (R) V.8.4, and verified using the results of experimental studies carried out using the UK Carbon Capture and Storage Research Centre/Pilot-scale Advanced Capture Technology (UKCCSRC/PACT) pilot plant, as a representative pilot-scale capture plant, and employed for parametric sensitivity studies. Several parameters have been identified and varied over a given range of lean solvent CO2 loading to evaluate their effects on the pilot plant energy requirement. The optimum lean solvent CO2 loading was determined using the total equivalent work concept. Results show, for a given packing material type, the majority of energy savings can be realised by optimising the stripper operating pressure. To some extent, a higher solvent temperature at the stripper inlet has the potential to reduce the regeneration energy requirement. A more efficient packing material, can greatly improve the pilot plant overall energy and mass transfer efficiency. (C) 2016 Elsevier Ltd. All rights reserved.
引用
收藏
页码:243 / 253
页数:11
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