Global cost optimization of a mini-scale liquefied natural gas plant

被引:33
作者
Aslambakhsh, Amir Hamzeh [1 ]
Moosavian, Mohammad Ali [2 ]
Amidpour, Majid [3 ]
Hosseini, Mohammad [4 ]
AmirAfshar, Saeedeh [5 ]
机构
[1] IPMI, Commercial Dept, Piping & Instrumentat Disciplines, Saadat Abad Ave, Tehran, Iran
[2] Univ Tehran, Coll Engn, Sch Chem Engn, Tehran, Iran
[3] KN Toosi Univ Technol, Dept Mech Engn, Pardis St,Mollasadra Ave,Vanak Sq, Tehran 1999143344, Iran
[4] Iranian Oil Terminal Co, Oil Lab, Asaluyeh 75119158, Iran
[5] Univ Tehran, Coll Engn, Sch Chem Engn, Inst Liquefied Nat Gas I LNG, Tehran, Iran
关键词
Mini LNG plant; Single mixed refrigerant; PRICO process; Optimization; Genetic algorithm; Exergy analysis; LOW-TEMPERATURE PROCESSES; EXERGY; LNG; ALGORITHM; DESIGN; SINGLE;
D O I
10.1016/j.energy.2018.01.127
中图分类号
O414.1 [热力学];
学科分类号
摘要
Cryogenic natural gas liquefaction plant has huge capital and operating expenses corresponding to operating equipment and energy utilization. Considering ever-increasing energy price, therefore, minimization of energy consumption rate for a better profit is highly required. However, any un-engineered energy cut off would result in larger surface area of heat-exchanger and hence bigger capital cost. Here, the net profit of establishing a mini 50 ton/day liquefied natural gas facility, operating for 25 years, is optimized via Genetic Algorithm technique. Poly Refrigerant Integrated Cycle Operations (PRICO) process is simulated in HYSYS environment and linked to MATLAB software for subsequent maximization. The simulation resulted in total consumed power, heat exchanger area and total profit by 274533 kW, 3285.58 m(2) and 1266.64 million$, respectively. In order to determine unit efficiency and plant irreversibility rate, exergy analysis is performed on individual equipment. Basically, thirteen independent variables are considered for optimization of objective function. Sensitivity analysis for objective function is considered by altering each variable. Final results indicate 9.26% rise in total profit (1383.95 million$) by 59% reduction in energy utilization (1127.68 kW) and 37.50% in heat-exchanger size (2053.7 m(2)). Meanwhile, the total and heat-exchanger exergy losses are decreased by 65.8% and 80.7%, respectively. (C) 2018 Elsevier Ltd. All rights reserved.
引用
收藏
页码:1191 / 1200
页数:10
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