Transient tests on blower trip and rod removal at the HTR-10

被引:25
|
作者
Hu, S [1 ]
Wang, R [1 ]
Gao, Z [1 ]
机构
[1] Tsing Hua Univ, Inst Nucl Energy Technol, Beijing 102201, Peoples R China
关键词
D O I
10.1016/j.nucengdes.2005.11.015
中图分类号
TL [原子能技术]; O571 [原子核物理学];
学科分类号
0827 ; 082701 ;
摘要
Safety demonstration tests on the 10 MW high temperature gas-cooled reactor test module (HTR-10) were conducted to verify the inherent safety features of MHTGRs and to obtain the core and primary cooling system transient data for validation of safety analysis codes. Two simulated anticipated transients without scram (ATWS) tests, lose of forced cooling by trip of the helium blower and reactivity insertion via control rod withdrawal were performed. This paper describes the tests with detailed test method, condition and results. Calculated results show that the strongly negative temperature coefficient causes reactor power to closely follow heat removal levels. Maximum fuel temperature changes are limited by the large core heat capacity to below 1230 degrees C during two tests. The test of tripping the helium circulator ATWS test was conducted on October 15, 2003. Although none of 10 control rods was moved, the reactor power immediately decreased due to the negative temperature coefficient. After about 50 min, the reactor became criticality again. Finally, the reactor power went to a stable level with about 200 kW. The test of reactivity insertion ATWS test was conducted two times. Following the control rod withdrawal, the reactor power increased rapidly, the maximum power level reached to 5037 and 7230 kW from the initial power of 3000 kW in accordance with reactivity insertion of $0.136 and 0.689, respectively. After the reactivity introduced was compensated by means of the strong negative reactivity feedback effect, the reactor went to subcritical and the power decreased. (c) 2006 Elsevier B.V. All rights reserved.
引用
收藏
页码:677 / 680
页数:4
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