A novel modification on preheating process of natural gas in pressure reduction stations to improve energy consumption, exergy destruction and CO2 emission: Preheating based on real demand

被引:29
作者
Olfati, Mohammad [1 ,2 ]
Bahiraei, Mehdi [3 ]
Veysi, Farzad [1 ]
机构
[1] Razi Univ, Dept Mech Engn, Fac Engn, Kermanshah, Iran
[2] NIGC, Tech & Engn Dept, Kermanshah, Iran
[3] Kermanshah Univ Technol, Dept Mech Engn, Kermanshah, Iran
关键词
Pressure reduction station modification; Energy performance improvement; Real demand; Heater CO2 emission; Exergy destruction; Natural gas; HEAT; OPTIMIZATION; TEMPERATURE; GENERATION; SYSTEMS;
D O I
10.1016/j.energy.2019.02.090
中图分类号
O414.1 [热力学];
学科分类号
摘要
One of the tools for optimizing energy systems is the design of the system output based on real (desired) demand. Thermodynamic performance of natural gas pressure reduction stations are functions of inlet conditions. In order to investigate the impacts of changes in inlet pressure and temperature on performance of a natural gas pressure reduction station, energy consumption and exergy destruction of a natural gas pressure reduction station of 10,000 SCMH are evaluated for different inlet conditions. In order to improve the station performance, a novel modification is proposed in the present research based on the real demand of preheating, wherein thermodynamic operation of the regulator is modeled and minimum pre-heating temperature of natural gas is calculated based on desirable temperature at the regulator outlet (natural gas hydrate formation temperature). Indeed, once the temperature at the heater outlet reaches the calculated minimum temperature, the heater is turned off. Compared to conventional stations, the modified station exhibits at least 33% and 15% reductions in energy consumption and exergy destruction, respectively. The results of investigating the performance of two sample stations also show that by implementing the proposed modification, CO2 emission can be reduced by up to 80% or even higher. (C) 2019 Elsevier Ltd. All rights reserved.
引用
收藏
页码:598 / 609
页数:12
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