Simulation and Economic Benefit Analysis of Carburetor Combined Transport in Winter at a Liquefied Natural Gas Receiving Station

被引:2
作者
Cao, Song [1 ]
Luan, Tao [2 ]
Zuo, Pengliang [2 ]
Si, Xiaolei [2 ]
Xie, Pu [3 ]
Guo, Yingjun [1 ]
机构
[1] Hebei Univ Sci & Technol, Sch Elect Engn, Shijiazhuang 050027, Peoples R China
[2] Caofeidian Xintian LNG Co Ltd, Tangshan 063200, Peoples R China
[3] Tianjin Renai Coll, Sch Informat & Intelligent Engn, Tianjin 301636, Peoples R China
关键词
liquefied natural gas; open rack vaporizer; submerged combustion vaporizer; economic optimization; seawater flow optimization;
D O I
10.3390/en18020276
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
In the winter, a certain LNG receiving terminal operates exclusively with the submerged combustion vaporizer (SCV). However, due to the high operational costs associated with the SCV, a new combined operation scheme utilizing both the SCV and the open rack vaporizer (ORV) has been proposed. First, models for the SCV and ORV gasification units were developed in Aspen HYSYS and validated using actual operational parameters. Next, the relationship between the seawater inlet-outlet temperature difference and the minimum seawater flow rate for the ORV was determined, and an optimized seawater pump operation strategy, considering LNG export volumes, was formulated. Additionally, the relationship between the SCV fuel gas flow rate and LNG export volume was analyzed, and a comparison was made between the operating costs of SCV running independently and the combined SCV-ORV operation under winter conditions. The results of the combined operation experiments indicated that at a seawater inlet-outlet temperature difference of 3 degrees C, the joint operation mode could save costs by 70-77%; at 2.5 degrees C difference, it saves 60-67%; at 2 degrees C difference, it saves 45-50%; at 1.5 degrees C difference, it saves 35-38%; and at 1 degrees C difference, it saves 20-23%. This approach achieves optimized economic performance for LNG terminal operations.
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页数:14
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