Development of a Large Mass Flow Inlet Test System in Low Speed Wind Tunnel

被引:0
|
作者
Tang B.-B. [1 ]
Li C.-K. [1 ]
机构
[1] The 3rd Aerodynamic Research and Test Department, AVIC Aerodynamics Research Institute, Harbin
来源
关键词
Ejecting; Inlet; Large mass flow; Performance measurement; Wind tunnel test;
D O I
10.13675/j.cnki.tjjs.2018.12.024
中图分类号
学科分类号
摘要
A large mass flow inlet test system was developed in the FL-8 wind tunnel to improve its test ability. According to the condition, the system was set in the center of the wind tunnel and ejected mixed air into the diffusion section without destroying the original one. The system can perform all kinds of inlet test functions including inlet flow field simulation, performance measurement, flow control and measurement. In order to verify the performance of the system, a test was carried out. Results show that the system has high measurement accuracy, ejection ability and exhaust air has little influence on the wind tunnel flow field. The flow measurement accuracy achieve 0.3% and the inlet test system achieves maximum 2.8kg/s, which leads to a 50% capacity increase and can carry out three inlet test simultaneously. © 2018, Editorial Department of Journal of Propulsion Technology. All right reserved.
引用
收藏
页码:2839 / 2844
页数:5
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