110 kV Artificial Short-circuit Test and Result Analysis of Wind Power Base in Xinjiang Power Grid of China

被引:0
|
作者
Peng Y. [1 ]
Wang H. [1 ,2 ]
Wang W. [1 ,2 ]
Nan D. [1 ,2 ]
Qi X. [3 ]
Yang Y. [4 ]
机构
[1] School of Electrical Engineering, Xinjiang University, Urumqi
[2] Research Center of Renewable Energy Power Generation and Grid Control Engineering, Ministry of Education, Xinjiang University, Urumqi
[3] Electric Power Research Institute of State Grid Xinjiang Electric Power Co., Ltd., Urumqi
[4] Electric Power Research Institute of State Grid Jiangsu Electric Power Co., Ltd., Nanjing
来源
Wang, Haiyun (327028229@qq.com) | 1600年 / Automation of Electric Power Systems Press卷 / 44期
基金
中国国家自然科学基金;
关键词
Artificial short-circuit test; Calculation model; Relay protection; Short-circuit current; Wind power;
D O I
10.7500/AEPS20190617007
中图分类号
学科分类号
摘要
In order to weaken the dependence on fossil energy and develop renewable energy sources, the installed capacity of wind power in Xinjiang in China has been increasing year by year. At the same time, the impact of large-scale wind power integration on the traditional distribution network is increasingly significant, especially the short-circuit current when the short-circuit fault occurs, which reduces the reliability of the relay protection and result in instability of the power system. The 110 kV artificial short-circuit test of Xinjiang Power Grid not only carries out the preparation of detailed test plan, but also analyzes the influencing factors of short-circuit current. The analysis of calculated value and test value error based on PSASP power flow mode is implemented. At last, the degree of fit between the different types of wind turbine calculation models of the current power system and the actual situation of the power grid. The error ratio between the calculated current and the measured current with different fault types are obtained, and the influencing factors of the calculated values and the measured values are summarized. © 2020 Automation of Electric Power Systems Press.
引用
收藏
页码:226 / 231
页数:5
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