Erskine field HP/HT workover and tubing failure investigation

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作者
Mowat, D.E.
Edgerton, M.C.
Wade, E.H.R.
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| 1600年 / Society of Petroleum Engineers (SPE)卷 / 53期
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Failure (mechanical) - Oil fields - Oil well drilling - Packers - Stainless steel - Stress corrosion cracking - Tubing;
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摘要
The first workover of a U.K. North Sea high-pressure/high-temperature (HP/HT) production well was completed successfully in August 1999. The workover in Erskine field was the result of failure of the duplex stainless-steel (DSS) production tubing in the through-water zone. Tubing failure was attributed to external chloride stress corrosion cracking (SCC) in the annulus vapor space above a calcium chloride (CaCl2) packer fluid. Although some details of the failure mechanism remain uncertain, the full-length paper presents available information to assist future HP/HT-well designers.
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页码:68 / 71
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